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| | #1 (permalink) |
| temporarily on-hold Paid Member | It was running really good . . . . . . and then it wasn't. It's essentially winter in Ohio and I thought my 93 was tucked away in the garage for the season (it is supposed to snow 3-5 inches tonight). Since the turbo install, I have been running NGK TR5 plugs. Since there was no Ohio State football on this afternoon, I decided I would spend the time by installing some NGK TR6 plugs. Well, after I got them in, I looked outside and it hadn't started to snow yet, the roads were dry, and there was still about a half-hour of daylight left. So then, I had to take it out for a little post-plug installation test drive. It was running great, but it was starting to get dark, so I decided to turn around and head for home. After I turned it around, I gave it enough throttle to burn the tires through first and as I was burning the tires through second, all of a sudden . . . BANG! It immediately lost power, but didn't seize up. At first, I thought that I could limp it home, but only made it about a quarter-mile before it died. I popped the hood to take a look, but it was kind of dark out and I didn't have a flashlight. I tried to start it and it kind of acted like it wanted to start, but it wouldn't. The fuel pressure was good before the battery died. As I was waiting for the tow-truck, I was thinking to myself that the engine could be rebuilt better than ever (forged internals, new cam, roller rockers, aluminum heads, etc.). We got it into the garage and I started charging the battery. I then got out the "troublelight" and started to look around. Almost immediately, I noticed that the silicone coupler between the turbo discharge tube and the intercooler influent was disconnected - definitely a good sign! I hooked it back up, started it back up, and all is well! For as loud as that "bang" was, I think the coupler was on pretty tight. Has anybody else blown an intercooler line off like this before? There must have been some decent back- pressure built up. Do you suppose that this post belongs in the "BOV hell..." thread? Any other thoughts? I was not at WOT when it happened, but I might have been feathering the throttle to keep the tires spinning. ![]()
__________________ 1993 #4572, MP T-70 Turbo, Pickrel Turbo Exhaust, PSD Intercooler, PSP MAF kit w/SCT Chip & BA 2400, 42# Injectors, Dual Pump Trick, 255 Inline, LFP Traction Bars, B&M Transpak w/deep pan, FMS Girdle, LaSota Racing Tuned, 400 RWHP/460 RWTQ, Zaino Shine, TBD |
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| | #2 (permalink) |
| Gen 1 Salvage Yard Owner Paid Member | Glad i read the whole post first i was just about to tell you check all the silicone coupler's. I have seen it happen on a friends truck a couple times. Well glad it was'nt anything serious. Bobby |
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| | #4 (permalink) |
| Boost Kills !!!!!!! Join Date: Jul 2002 Location: Oxford, Alabama
Posts: 2,640
View this user's gallery iTrader: 24 / 100% | Whew....you scared me for a minute. Glad it was just a coupler.
__________________ SOLD - 2003 Lightning # 1180 SOLD - 1993 Lightning # 5173 ![]() 2005 Pontiac GTO 2004 Mustang Mach1 2004 Chevy 2500HD 4x4 CrewCab Diesel |
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| | #6 (permalink) |
| temporarily on-hold Paid Member | I really thought something expensive had broken, but I didn't feel all that queezy about it. I was more concerned about getting it back into the garage before it started to snow. My Lightning is just a toy and the turbo makes it so much fun to play with. I don't drive it very often, but when I do, staying out of the boost is not an option - I'm pretty sure that it is just a matter of time that something major will go south. |
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| | #7 (permalink) | |
| temporarily on-hold Paid Member | Quote:
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| | #8 (permalink) |
| Senior Member | Hey Jim, The clamps you have are consistant torque and are better than the T- bolt type clamps... All the washers you see on them act like a spring allowing them to maintain a more consistant grip through the expanding and contracting that goes on... You probably just need to tighten the clamps a little more than it was on the connection that came loose and it should be fine... If it happens again you can use two clamps on the side of the connection that came loose... Since you have stock motor mounts your motor moves a lot when jump on and off the throttle and this doesent help the situation... Also make sure your drivers side motor mount is still in one piece... it is very common for them to come apart... TTYL, Dave |
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| | #10 (permalink) |
| Grasshoppa' Join Date: Feb 2001 Location: Demotte, IN/Escanaba, MI
Posts: 872
View this user's gallery iTrader: 0 / 0% | You can also run link bars in many applications to hold the tubes together to avoid that situation. |
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| | #12 (permalink) |
| Vrrooooooooooom | I had that happen several times back in the supercharger days. First time it happened, I'd just put a new set of heads on and was out testing when it happened. I had no tools with me, was wearing a pair of shorts, a t-shirt with holes in it, and no shoes. I was thinking, "Man, that's a long walk home barefoot." I was pretty relieved when I popped the hood and saw the separated tubes! |
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| | #14 (permalink) |
| Senior Member | Jim, You can buy the clamps from here http://intakehoses.com you need a CT-350 for a 3" ID hose... TTYL, Dave |
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