The National Lightning Owners Club Inc The National Lightning Owners Club Inc
 
Home |  Classified Ads |  Gallery |  Join the Club |  Register on the Forum |  Merchandise |  Supporting Vendors |  Chat 

Go Back   The National Lightning Owners Club Inc > The Trucks > Legacy Threads 2000-2002 -- The Old NLOC Website > The Trucks - Old NLOC Website, 2000-2002 > Gen 1 Lightnings - legacy

 
 
LinkBack Thread Tools Display Modes
Old 09-02-2001, 09:46 AM   #1 (permalink)
Litl Sam
Guest
 
iTrader: / %
Angry The L had to be towed home! Need some help!

Shut off on me going down the interstate. Starts for a split second but shuts right off. Smoke out the exhaust. Any ideas what to look at or for? Going to take a look at it now but any thoughts you guys have will be appreciated. Thanks

------------------
Sam Sells
NLOC#617
'95 #1325
Powerdyned
13.555@101.38
 
Old 09-02-2001, 10:01 AM   #2 (permalink)
HotRod
Guest
 
iTrader: / %
Post

I dont like the smoke out the exhaust, as that could be a head gasket. So, can you give a little more detail, Sam? Did it start to sputter or just quit? Were you at 10psi of boost or cruising? First Id check all of your connections for the ignition/coil. Make sure your blower tube didnt get blown off. All the vaccume lines and see if you have fuel pressure on your guage. Check all of the normal stuff, oils and see what you have. Im sure we'll figure this out.
That sucks having to get towed home. Rod K.

------------------
Rod K.

'93 Lightning #1529
13.683 @ 98.66 Au Natural
'98 SVT Contour E1 #5782
'00 Suzuki Bandit S1200 10s??

[This message has been edited by HotRod (edited 09-02-2001).]
 
Old 09-02-2001, 10:07 AM   #3 (permalink)
Litl Sam
Guest
 
iTrader: / %
Post

I was cruising(no boost). It might have sputtered but I think it shut right off. It starts to crank but then it is like it stalls. I didn't think there was any codes but I am getting:
542 (O,M) Fuel pump open, bad ground or always on ﷓ ﷓ Power / Fuel Pump Circuits
556 (O,M) Fuel pump relay primary circuit fault ﷓ Power / Fuel Pump Circuits
 
Old 09-02-2001, 10:30 AM   #4 (permalink)
gadrix
Guest
 
iTrader: / %
Post

Could be fuel pressure regulator failure.
Don't know how modded you L is. My regulator failed and the high fuel pressure caused an extreme rich condition to the point of smoke out the exhaust from unburned fuel and stumbling.
If stock, this is a currently recalled item.
 
Old 09-02-2001, 10:59 AM   #5 (permalink)
Muddmann
Guest
 
iTrader: / %
Question

didja try and switch tanks? maybe pump failure...but surely not both of em at same time

------------------
if i stop runnin, the evil little clowns will get me...
 
Old 09-02-2001, 11:12 AM   #6 (permalink)
gasguzzler
Guest
 
iTrader: / %
Post

What color was the smoke?
 
Old 09-02-2001, 11:33 AM   #7 (permalink)
SVT-FAN
Guest
 
iTrader: / %
Unhappy

Sorry to hear about your problems!!!!!!!!!!Hope its not to bad
 
Old 09-02-2001, 06:40 PM   #8 (permalink)
Litl Sam
Guest
 
iTrader: / %
Post

Ok boys, prepare to laugh! I had disconnected by bypass for something monday. I forgot to tighten a screw that held the discharge tube in at the throttle body. I can't believe I didn't see it hanging off when I was on the side of the road. I got my dad to come over to help me push it in garage and showed him what it was doing. The hood was up and he said, "did you disconnect this"? All I could say was hell yeah.........MONDAY! I'm a DORK! Thanks for the fast responses when I thought there was a problem!

Let the jokes begin!

------------------
Sam Sells
NLOC#617
'95 #1325
Powerdyned
13.555@101.38
 
Old 09-02-2001, 09:01 PM   #9 (permalink)
HotRod
Guest
 
iTrader: / %
Talking

Goober! I told you to check you discharge tube!! Geez!! They dont run too good like that, do they? Glad you found the problem, Rod K.

------------------
Rod K.

'93 Lightning #1529
13.683 @ 98.66 Au Natural
'98 SVT Contour E1 #5782
'00 Suzuki Bandit S1200 10s??
 
Old 09-02-2001, 09:03 PM   #10 (permalink)
Blue Oval Forever
Guest
 
iTrader: / %
Post

No Jokes Sam it happens to the best of us

------------------
Bobby
95 Lightning Red #233
14.65 @90 MPH
New mods coming soon hunting the 12 sec. zone
Born on 01\03\95
86 Mustang Coupe 351c
93 Convertible
NLOC #500
Ford Performance Association Member
http://members.aol.com/rjdruhan/FPA/fpa.htm
 
Old 09-02-2001, 10:07 PM   #11 (permalink)
TraumaPirate
Guest
 
iTrader: / %
Question

Ok, since I'm not blown, I don't understand why the discharge tube not being connected would make a difference.
I know some of y'all take the blower belt off and run a cone filter on the TB during long trips, so if it runs this way, why wouldn't it run if the discharge tube is disconnected?

------------------
John
 
Old 09-03-2001, 11:13 AM   #12 (permalink)
sstock
Guest
 
iTrader: / %
Post

Ditto here, cant understand why that would stop anything, just getting unfiltered air thats all??????

------------------
94 Crimson #2826
Born May 6, 1994
NLOC member #343
Team Powerdyne,
13.49@ 102mph
Wanting 12's

'GREASED'
 
Old 09-03-2001, 03:16 PM   #13 (permalink)
MO351
Guest
 
iTrader: / %
Cool

Could it be that he was getting way too much fuel and not enough air to go with the mixture and therefore the motor wouldn't run? Flooded out or something?

------------------
Adam B.
1994 Red SVT Lightning #2019
 
Old 09-03-2001, 04:17 PM   #14 (permalink)
huffentuff95
Guest
 
iTrader: / %
Lightbulb

Don't feel bad, we all have had a brain fart at one time or another. I could remember changing the oil in my 1977 750 honda and putting the plug in the oil tank hand tight. This was many moons ago. Well to make a long story short I was cruising down the road on a late night and I saw the oil light blink on a few times, good thing for idiot lights. It then came on and stayed on , so I pulled over. You could see the oil trial on the road for as far as I could see. Bummer was I had to push the bike 2 miles to a store with a phone to get help. Cell phone ? what was that back then. Never found the drain plug and I looked. I felt like a fool too but at least I didn't hurt my bike.

------------------
Dennis Macho
95 RED
NLOC #277
13.38 @ 102.71 unhooked
 
Old 09-03-2001, 04:47 PM   #15 (permalink)
Litl Sam
Guest
 
iTrader: / %
Post

Well the tube hanging off was kinda blocking the inlet to the throttle body. When I got it home and tried to crank it, same thing, it would fire up but then shut right off. It sat for a little bit while I was checking the site. I called my dad to come over and help me push it in the garage. Started it so he could see what it was doing and it started but just barely stayed running, putting out alot of smoke. The hood was open at this time and that was when he saw it was hanging loose and asked if/why I had that off. I think with it blocking the inlet and all the heat it didn't get enough air. Once it sat alittle bit the air was cooler enough just so it would barely run. Thats what I guess. I will definatly check all screws for tightness now.

------------------
Sam Sells
NLOC#617
'95 #1325
Powerdyned
13.555@101.38
 
 

Thread Tools
Display Modes

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off
Trackbacks are On
Pingbacks are On
Refbacks are On

Forum Jump


All times are GMT -5. The time now is 06:30 PM.


Powered by vBulletin®
Copyright ©2000 - 2010, Jelsoft Enterprises Ltd.
SEO by vBSEO 3.2.0
Copyright NLOC, Inc. 2001-2009