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Old 02-12-2009, 06:26 PM   #1 (permalink)
wildman
 
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KB failure

Well accepting the truth after I tried for 2 days to make this thing work, I give up. Game over, throwing in the towel calling it quits! Here is the deal. All my fabricated parts(midplate-plenum) worked awesome didn't leak or anything so I can say I did something right but I got the truck running with the KB on it and the blower just kept getting louder and louder and tighter too. Soooooo it was locking up on me. After I took the blower apart again I noticed the rotors were still dragging the case. Its repairable with the right tools to smooth the cases but bottom line is that I want a blower that will last as long as the truck does so I decided to spend the cash once instead of "home making" a S/C kit. Whipple 2.3 here I come! Well Im comin whipple but it may take a few months so Im finally putting this project to rest and Im just gonna have to settle for a damn eaton for a while. Oh well. The project wasn't a complete failure, I made friends in the process and I learned how to fabricate and weld. Hopefully I can get 3/4 of my money out of it but whatever live and learn. Can't say I didn't try and at least I admit my mistakes. See yall in oldtown better an eaton than nothin at all.
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Old 02-12-2009, 11:27 PM   #2 (permalink)
SilverL
 
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lol goodluck and what are u gunna do with old kb?
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Old 02-13-2009, 06:29 AM   #3 (permalink)
Boosted by Whipple
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That sucks, It sounds like the boost actuator wasn't working.
__________________
...........04 DSG, Built 9/02/03 #53/3781...........
............Tuned by JDM, 10.23 @131.98.............
..................2.3 Whipple/ No Spray...................
......2007 Moroso Truck Series Champion......
........2009 PBIR Truck Series Runner Up.......
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Old 02-14-2009, 06:02 PM   #4 (permalink)
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Boost bypass was fine and the kb is on ebay for sale as is needs to be rebuilt.
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